TY - JOUR
T1 - Effect of sulphate addition on volatile fatty acid and ethanol degradation in an anaerobic hybrid reactor. I
T2 - Process disturbance and remediation
AU - O'Flaherty, Vincent
AU - Colleran, Emer
PY - 1999/5
Y1 - 1999/5
N2 - The addition of sulphate (4 g/l) to the influent of a mesophilic (35 ± 2°C) laboratory-scale anaerobic hybrid reactor (volumetric loading rate 6 kg/m3/day) treating a propionate-, butyrate- and ethanol-containing (1:1:1 on a COD basis; total COD of 12 g/l) wastewater resulted in severe process disturbance, with a complete inhibition of the propionate-degrading ability of the sludge. Severe inhibition of acetate removal was also observed, with concentrations of propionate and acetate in the reactor effluent of 4000 and 1000 mg/l, respectively. An oscillating pattern of sulphate and sulphide concentrations was observed in the reactor effluent. A control reactor, which had no influent sulphate, maintained a COD removal efficiency of > 95% throughout the trial period. A number of remediation strategies were undertaken with the sulphate-fed reactor. Initially, the levels of total sulphide in the digester were reduced to < 500 mg/l from peak values of > 1000 mg/l by inclusion of a nitrogen gas sparging system at 4.12 l/l/day (5.36 l/m2/day). Although the levels of total sulphide were reduced in the reactor, little improvement in COD removal was observed. Re-inoculation of 21 of non-sulphate-adapted seed sludge (25 g VSS/l; 6.0% inoculum) into the digester did not improve the reactor performance either, suggesting that no improvement could take place in the absence of appropriate sulphate-reducing bacteria or sulphate-adapted syntrophic and methanogenic bacteria. Successful bioaugmentation of the reactor was achieved by the inoculation of 21 sulphate-adapted sludge (25 g VSS/l; 6.0% inoculum) from a full-scale digester. Improvement in reactor performance was observed after one retention time (48 h) and the COD removal efficiency exceeded 95% by the conclusion of the trial.
AB - The addition of sulphate (4 g/l) to the influent of a mesophilic (35 ± 2°C) laboratory-scale anaerobic hybrid reactor (volumetric loading rate 6 kg/m3/day) treating a propionate-, butyrate- and ethanol-containing (1:1:1 on a COD basis; total COD of 12 g/l) wastewater resulted in severe process disturbance, with a complete inhibition of the propionate-degrading ability of the sludge. Severe inhibition of acetate removal was also observed, with concentrations of propionate and acetate in the reactor effluent of 4000 and 1000 mg/l, respectively. An oscillating pattern of sulphate and sulphide concentrations was observed in the reactor effluent. A control reactor, which had no influent sulphate, maintained a COD removal efficiency of > 95% throughout the trial period. A number of remediation strategies were undertaken with the sulphate-fed reactor. Initially, the levels of total sulphide in the digester were reduced to < 500 mg/l from peak values of > 1000 mg/l by inclusion of a nitrogen gas sparging system at 4.12 l/l/day (5.36 l/m2/day). Although the levels of total sulphide were reduced in the reactor, little improvement in COD removal was observed. Re-inoculation of 21 of non-sulphate-adapted seed sludge (25 g VSS/l; 6.0% inoculum) into the digester did not improve the reactor performance either, suggesting that no improvement could take place in the absence of appropriate sulphate-reducing bacteria or sulphate-adapted syntrophic and methanogenic bacteria. Successful bioaugmentation of the reactor was achieved by the inoculation of 21 sulphate-adapted sludge (25 g VSS/l; 6.0% inoculum) from a full-scale digester. Improvement in reactor performance was observed after one retention time (48 h) and the COD removal efficiency exceeded 95% by the conclusion of the trial.
KW - Acetate
KW - Anaerobic digestion
KW - Bioaugmentation
KW - Hybrid reactor
KW - Methanogenic bacteria
KW - Process disturbance
KW - Propionate
KW - Sulphate-reducing bacteria
KW - Sulphide
UR - http://www.scopus.com/inward/record.url?scp=0033135886&partnerID=8YFLogxK
U2 - 10.1016/S0960-8524(98)00145-X
DO - 10.1016/S0960-8524(98)00145-X
M3 - Article
SN - 0960-8524
VL - 68
SP - 101
EP - 107
JO - Bioresource Technology
JF - Bioresource Technology
IS - 2
ER -